Ok guys, after replacing the powerhead gasket here are the results of the DDT test and pressure tests...
The only faults were SmartGauges that I didnt have hooked up like fuel, oil, tach, pitot, etc. an overreving, an overheat, and also a TPI Circuit to low. When he did the misfire tests (shutting down the cylinders one at a time) the #2 cylinder didnt do anything. So, he switched the plug wires...didnt fix it...switched the coil...didnt fix it...switched the coil driver...didnt fix it...switched the fuel injectors...didnt fix it...switched the air injectors...didnt fix it...took the pulse fuel pump apart and replaced the diaphram and gaskets...didnt fix it...tried new plugs...didnt fix it...all the continuity tests were good also. We did notice that the #2 fuel injector was perfectly clean but the others had black carbon on them...it's like there is too much fuel being dumped into the #2 cylinder and it's fouling the plug. So, I'm back at square 1!!! Still only reving 4950 RPM at WOT
Tags: