1993 Dodge Caravan 3.0L V6 problem started with blown head gasket. I replaced and torqued head. After assembly and started vehical, it ran like it has a terrble misfire. It ran absolutely great and smooth before all this happened to me. Then a relative told me the intake bolts had to be torequed in sequence to the book. I tore it all apart again to torque the bolts on lower part of the MFI Intake to 15lbs. then realized I did this after the permatex gasket sealer had dried...Do you think this would have made a difference? and The Oxygen Sensor wire was cut when I tried to hack saw the manifold studs off to replace them. So the Oxygen sensor isnt connected, after reading lots of stuff online about Oxygen sensors making cars run rough, and rich, etc. I'm now wondering is the cause of all this the Oxygen Sensor, or the Intake Gaskets being re-tightened after permatex dried overnight? I did spray some WD40 all around the intake seal while running it, and there was no change in idle, as checking for air leaks etc. I know its not a misfire, we timed it correctly, and gave it full tune up as well?
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